Bridgeport CNC Mill: Difference between revisions
From Pumping Station One
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The homing sequence could not complete due to a bad index signal from the y axis rotary encoder. By adjusting the alignment of the encoder to the motor, the signal appeared. This adjustment may need attention in the future. | The homing sequence could not complete due to a bad index signal from the y axis rotary encoder. By adjusting the alignment of the encoder to the motor, the signal appeared. This adjustment may need attention in the future. | ||
The handwheel problem was caused by user error. Ryan discovered that the sequence to use the handwheel is: 'handwheel', axis, 'enter'. We weren't pushing 'enter'. | |||